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Corporate Information

 
Press Release (Dec 19,2011)
Plant Status of Fukushima Daiichi Nuclear Power Station (as of 10:00 am, December 19)
 
*Updates are underlined. 
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down. 
Unit 1 (Shut down) 
-Explosive sound and white smoke were confirmed after the big quake 
 occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
-At 3:37 pm on March 25, we started injecting freshwater to the reactor 
 and are now injecting fresh water by a motor driven pump powered by the 
 off-site transmission line. 
-At 10:11 am on December 10, in addition to water injection from water 
 feeding system, we started water injection from piping of core spray 
 system to the reactor.
 The current water injection volume is approx 4.8 m3/h from the reactor 
 feed water system and approx. 2.0 m3/h from the core spray system.
-We commenced injection of nitrogen gas into Primary Containment Vessel at 
 1:31 am on April 7.
-At 11:22 am on August 10, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System. 
-On October 28, we completed installation of the cover for the Reactor 
 Building in order to contain dispersion of radioactive substances.
-At 4:04 pm on November 30, we started operation to inject nitrogen into 
 the reactor pressure vessel. 
Unit 2 (Shut down) 
-At approximately 6:00 am on March 15, an abnormal noise began emanating 
 from nearby Pressure Suppression Chamber and the pressure within the 
 chamber decreased. 
-At 10:10 am on March 26, we started injecting freshwater to the reactor 
 and are now injecting fresh water by a motor driven pump powered by the 
 off-site transmission line. 
-At 2:59 pm on September 14, in addition to water injection from water 
 feeding system, we started water injection from piping of core spray 
 system to the reactor.
 The current water injection volume is approx. 2.7 m3/h from the reactor 
 feed water system and approx. 6 m3/h from the core spray system. 
-At 5:21 pm on May 31, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System. 
-At 8:06 pm on June 28, we started injecting nitrogen gas into the Primary 
 Containment Vessel.
-From 6:00 pm on October 28, we put the gas management system of the 
 reactor containment vessel in operation.
-At 10:46 am on December 1, we started the nitrogen injection to the 
 Reactor Pressure Vessel. 
Unit 3 (Shut down) 
-Explosive sound and white smoke were confirmed at approximately 11:01 am 
 on March 14. It was assumed to be hydrogen explosion.
-At 6:02 pm on March 25, we started injecting fresh water to the reactor 
 and are now injecting fresh water by a motor driven pump powered by the 
 off-site transmission line.
-At 2:58 pm on September 1, we started water injection by core spray 
 system in addition to water injection by the reactor feed water system 
 piping arrangement. 
 The current water injection volume is approx 2.8 m3/h from the reactor 
 feed water system and approx. 5.8 m3/h from the core spray system.
-At 7:47 pm on June 30, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System.
-At 8:01 pm on July 14, injection of nitrogen gas into the Primary 
 Containment Vessel started. 
-At 4:26 pm on November 30, we started operation to inject nitrogen into 
 the reactor pressure vessel. 
Unit 4 (Outage due to regular inspection) 
-At around 6 am on March 15, we confirmed the explosive sound and the 
 sustained damage around the 5th floor rooftop area of Reactor Building.
-At 12:44 pm on July 31, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System.
-At 10:58 am on November 29, in order to decrease more salinity, we 
 installed Ion exchange equipment and started the operation of such 
 equipment.
-At this moment, we don't think there is any reactor coolant leakage 
 inside the primary containment vessel. 
Unit 5 (Outage due to regular inspection) 
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 5:00 am on March 19, we started the Residual Heat Removal System Pump 
 in order to cool the spent fuel pool.
-At 2:45 pm on July 15, we started the operation of the original Residual 
 Heat Removal System (System B) by its original seawater pump.
-At this moment, we don't think there is any reactor coolant leakage 
 inside the primary containment vessel. 
Unit 6 (Outage due to regular inspection) 
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 10:14 pm on March 19, we started the Residual Heat Removal System Pump 
 of Unit 6 to cool down Spent Fuel Pool.
-At 2:33 pm on September 15, we started separately cooling the reactor 
 through the Residual Heat Removal System and the spent fuel pool through 
 Equipment Cooling Water System and Fuel Pool Cooling System.
-At this moment, we do not think there is any reactor coolant leakage 
 inside PCV. 
Others 
-At around 10 am on June 13, we started the operation of the circulating 
 seawater purification facility installed at the screen area of Unit 2 and 
 3.
-At 8 pm on June 17, we started operation of Water Treatment Facility 
 against the accumulated water. At 6:00 pm on July 2, we started the 
 circulating injection cooling to inject the water, which was treated by 
 the accumulated water treatment system, to the reactors through the 
 buffer tank.
-At 7:41 pm on August 19, we started treatment of accumulated water by 
 parallel operation of one line from the cesium adsorption instrument to 
 the decontamination instrument and the other treatment line of the cesium 
 adsorption instrument No.2. 
-At 2:06 pm on October 7, we started to spray purified accumulated water 
 brought from Unit 5 and 6 continually in order to prevent dust scattering 
 and potential fire outbreaks from the cut down trees.
-On October 28, we started installation of the water proof wall at the sea 
 side, in front of the existing shore protection, Units 1-4, in order to 
 contain marine pollution by underground water.
-At 12:25 pm on December 13, we started the re-circulating operation of 
 desalination facility (reverse osmosis membrane type) for the purpose of 
 suppression of condensed water after desalination treatment.
-At 10:00 am on December 18, during the patrol activity, a TEPCO employee 
 found an accumulated water in the trench located between the process main 
 building of Centralized Radiation Waste Treatment Facility and 
 Miscellaneous Solid Waste Volume Reduction Treatment Building (High 
 Temperature Incinerator Building). The depth of the water was estimated 
 to be 50 cm and the amount was to be 125 m3. The radiation dose at the 
 water surface was 3 mSv/h (provisional value). As no radioactive 
 materials have been detected during the last sampling survey of sub drain 
 water near the trench, the source of the accumulated water is estimated 
 to be the ground water or dew condensation water. After that we found 
 water inflow from cable duct near the ceiling of the trench by detailed 
 survey at site, and we recalculated the amount of the accumulated water 
 and it was estimated to be approx. 230 m3. And as a result of the 
 sampling, Cesium-134 was approx. 4.2x103 Bq/cm3, Cesium-137 was approx. 
 5.4x103 Bq/cm3 and Iodine-131 was below detection limit regarding the 
 radioactivity density of the accumulated water in the trench, and 
 Cesium-134 was approx. 1.3x10-1 Bq/cm3, Cesium-137 was approx. 1.2x10-1 
 Bq/cm3 and Iodine-131 was below detection limit regarding the inflowing 
 water from cable duct. We have conducted water shut-off treatment of the 
 trench and the groundwater level is higher than the water level in the 
 trench, therefore we assumed that there is no possibility of inflow of 
 the accumulated water in the trench to the groundwater. We will conduct 
 investigation continuously and monitor the water level in the trench 
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