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Corporate Information

 
Press Release (Jan 09,2012)
Plant Status of Fukushima Daiichi Nuclear Power Station (as of 4:00 pm, January 9)
* The updates are underlined 
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down. 
Unit 1 (Shut down) 
- Explosive sound and white smoke were confirmed after the big quake 
  occurred at 3:36 pm on March 12, 2011. It was assumed to be hydrogen 
  explosion.
- At 3:37 pm on March 25, 2011, we started injecting freshwater to the 
  reactor and are now injecting fresh water by a motor driven pump powered 
  by the off-site transmission line. 
- At 10:11 am on December 10, 2011, in addition to water injection from 
  water feeding system, we started water injection from piping of core 
  spray system to the reactor.
  Current water injection volume is approx. 4.6 m3/h from the reactor feed 
  water system and approx. 1.8 m3/h from the core spray system.
- At 1:31 am on April 7, 2011, we commenced injection of nitrogen gas into 
  Primary Containment Vessel.
- At 11:22 am on August 10, 2011, we started cyclic cooling for the water 
  in the spent fuel pool by an alternative cooling equipment of the Fuel 
  Pool Cooling and Filtering System. 
- On October 28, 2011, we completed installation of the cover for the 
  Reactor Building in order to contain dispersion of radioactive substances.
- At 4:04 pm on November 30, 2011, we started operation to inject nitrogen 
  into the reactor pressure vessel.
- At 6:00 pm on December 19, 2011, a full-scale operation of the PCV gas 
  management system started. 
Unit 2 (Shut down) 
- At approximately 6:00 am on March 15, 2011, an abnormal noise began 
  emanating from nearby Pressure Suppression Chamber and the pressure 
  within the chamber decreased. 
- At 10:10 am on March 26, 2011, we started injecting freshwater to the 
  reactor and are now injecting fresh water by a motor driven pump powered 
  by the off-site transmission line. 
- At 2:59 pm on September 14, 2011, in addition to water injection from 
  water feeding system, we started water injection from piping of core 
  spray system to the reactor.
  At 10:04 am on January 9, 2012, because the replacement work of the water 
  injection piping arrangement from the water feed system in association 
  with the trial run of reactor injection pump in Turbine Building has been 
  completed, we have adjusted the amount of injected water to the reactor 
  gradually. For the amount of injected water to the reactor, we adjusted 
  water injection from the reactor feed water system from approx. 1.7 m3/h 
  to 3.0 m3/h, and water injection from the core spray system for approx. 
  8.1 m3/h to 7.0 m3/h. 
  Current water injection volume is approx. 3.0 m3/h from the reactor feed 
  water system and approx. 7.0 m3/h from the core spray system.
- At 5:21 pm on May 31, 2011, we started cyclic cooling for the water in 
  the spent fuel pool by an alternative cooling equipment of the Fuel Pool 
  Cooling and Filtering System.
- At 8:06 pm on June 28, 2011, we started injecting nitrogen gas into the 
  Primary Containment Vessel.
- At 6:00 pm on October 28, 2011, a full-scale operation of the PCV gas 
  management system started. 
- At 10:46 am on December 1, 2011, we started the nitrogen injection to 
  the Reactor Pressure Vessel. 
Unit 3 (Shut down) 
- Explosive sound and white smoke were confirmed at approximately 11:01 am 
  on March 14, 2011. It was assumed to be hydrogen explosion.
- At 6:02 pm on March 25, 2011, we started injecting fresh water to the 
  reactor and are now injecting fresh water by a motor driven pump powered 
  by the off-site transmission line.
- At 2:58 pm on September 1, 2011, we started water injection by core spray 
  system in addition to water injection by the reactor feed water system 
  piping arrangement. 
  Current water injection volume is approx 2.8 m3/h from the reactor feed 
  water system and approx. 6.1 m3/h from the core spray system.
- At 7:47 pm on June 30, 2011, we started cyclic cooling for the water in 
  the spent fuel pool by an alternative cooling equipment of the Fuel Pool 
  Cooling and Filtering System.
- At 8:01 pm on July 14, 2011, injection of nitrogen gas into the Primary 
  Containment Vessel started. 
- At 4:26 pm on November 30, 2011, we started operation to inject nitrogen 
  into the reactor pressure vessel. 
Unit 4 (Outage due to regular inspection) 
- At around 6 am on March 15, 2011, we confirmed the explosive sound and 
  the sustained damage around the 5th floor rooftop area of Reactor Building.
- At 12:44 pm on July 31, 2011, we started cyclic cooling for the water in 
  the spent fuel pool by an alternative cooling equipment of the Fuel Pool 
  Cooling and Filtering System.
- At around 1:00 pm on January 8, at circulating cooling system for spent 
  fuel pool of unit 4, we found water leakage from 4 points of cooling 
  pipe of air fin cooler (System B) when we tried to conduct scheduled 
  switching of air fin cooler (From System A to System B). Currently, we 
  are investigating the cause of the leakage. Leaked water is purified 
  water (pure water)* and is not contained radioactive materials. Now we 
  secluded the air fin cooler from the system to prevent the spread of 
  water leakage. In addition, the cooling of spent fuel pool has no problem 
  because we are currently using air fin cooler (System A) to cool spent 
  fuel pool.
  * Purified water (pure water): The water from Sakashita dam
- At 10:58 am on November 29, 2011, in order to decrease more salinity, we 
  installed Ion exchange equipment and started the operation of such 
  equipment.
- At this moment, we don't think there is any reactor coolant leakage 
  inside the primary containment vessel. 
Unit 5 (Outage due to regular inspection) 
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 5:00 am on March 19, 2011, we started the Residual Heat Removal System 
  Pump in order to cool the spent fuel pool.
- At 2:45 pm on July 15, 2011, we started the operation of the original 
  Residual Heat Removal System (System B) by its original seawater pump.
- At 10:11 am on December 22, 2011, since we finished the recovery work of 
  seawater pump (System B) of equipment water cooling system, we made a 
  trial run. At 11:25 am on the same day, we confirmed no abnormalities 
  and restarted the operation.
- At this moment, we don't think there is any reactor coolant leakage 
  inside the primary containment vessel. 
Unit 6 (Outage due to regular inspection) 
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 10:14 pm on March 19, 2011, we started the Residual Heat Removal 
  System Pump of Unit 6 to cool down Spent Fuel Pool.
- At 2:33 pm on September 15, 2011, we started separately cooling the 
  reactor through the Residual Heat Removal System and the spent fuel pool 
  through Equipment Cooling Water System and Fuel Pool Cooling System.
- At this moment, we do not think there is any reactor coolant leakage 
  inside PCV. 
Injured and others 
- At 2:22 pm on January 9, 2012, at the Spent Sludge Storage Facility (*) 
  which is under construction, a partner company's worker who had been 
  engaged in concrete placement work reported his physical disorder. He was 
  carried to the emergency medical room of Unit 5/6 and received medical 
  treatment. Because he was in cardiopulmonary arrest, he was carried from 
  Fukushima Daiichi Nuclear Power Station to Iwaki Kyouritsu Hospital at 
  3:25 pm. No radioactive materials were found to be attached to the worker's 
  body.  
  * Spent Sludge Storage Facility: The facility to store radioactive waste 
    (spent sludge), which is produced during the process of accumulated 
    water treatment, on a temporary basis. 
Others 
- At around 10 am on June 13, 2011, we started the operation of the 
  circulating seawater purification facility installed at the screen area 
  of Unit 2 and 3.
- At 8 pm on June 17, 2011, we started operation of Water Treatment 
  Facility against the accumulated water. At 6:00 pm on July 2, we started 
  the circulating injection cooling to inject the water, which was treated 
  by the accumulated water treatment system, to the reactors through the 
  buffer tank.
- At 7:41 pm on August 19, 2011, we started treatment of accumulated water 
  by parallel operation of one line from the cesium adsorption instrument 
  to the decontamination instrument and the other treatment line of the 
  cesium adsorption instrument No.2.
- At 2:06 pm on October 7, 2011, we started to spray purified accumulated 
  water brought from Unit 5 and 6 continually in order to prevent dust 
  scattering and potential fire outbreaks from the cut down trees.
- On October 28, 2011, we started installation of the water proof wall at 
  the sea side, in front of the existing shore protection, Units 1-4, in 
  order to contain marine pollution by underground water.
- At 12:25 pm on December 13, 2011, we started the re-circulating operation 
  of desalination facility (reverse osmosis membrane type) for the purpose 
  of suppression of condensed water after desalination treatment.
- At approximately 10:40 am on January 9, 2012, a water pond was found near 
  the evaporative concentration apparatus 2B (under suspension) of the water 
  treatment facility. The amount of the water is about 11 liter and is 
  staying in the dam. The leakage was from float type flow meter at vent 
  condenser spray line of evaporative concentration apparatus(*) and the 
  amount of leakage is about one drop in 6 seconds. After closing the valve 
  of the line, it was about one drop in 15 - 20 seconds. A dish will be 
  settled under the leakage. The water is purified one in evaporative 
  concentration apparatus (for water injection to the reactor). We conduct 
  nuclide analysis for the water of the line regularly and the last result 
  was as fallows: β -ray is 6.0×10-1Bq/cm3 (November 29, 2011) and γ -ray 
  is below measurable limit (December 20, 2011). 
  *Vent condenser spray line of evaporative concentration apparatus: 
   cooling the vapor (purified water) that is generated in the evaporative 
   concentration apparatus and supply water for injection to the reactor. 
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